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ADMIRAL 23" COLOR NO.1

admcolasfound
admcolasfound
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 THIS WAS A CURBSIDE FIND IN THE SUMMER OF 2005, IN GROVE CITY, OH.  I WAS GOING DOWN A RESIDENTIAL STREET AND SAW THIS ON THE CURB.  NATURALLY, I GRABBED IT.  ON INITIAL CHECK, THE CRT HAD ALMOST NO EMISSION, BUT IT CAME UP AFTER A LONG COOK.  I SOFT STARTED THIS AND ENDED UP GETTING A PICTURE.

  THE ELECTROLYTICS DID NOT REFORM TO MY SATISFACTION.  SEVERAL TUBES HAD HEATER/CATHODE LEAKAGE, AND WERE REPLACED.  FOR A WHILE, I USED THIS AS MY DAILY WATCHER.

   CHASSIS AFTER RECAPPING.  THE NEW LYTICS WERE HIDDEN UNDERNEATH AND THE OLD CANS DISCONNECTED.  IF I HAD IT TO DO OVER, I WOULD HAVE BOUGHT THE LYTICS FROM A DIFFERENT SUPPLIER, ONE THAT HAD ONES SMALL ENOUGH TO FIT IN THE CANS.  THE CLEAR PLASTIC MYLAR CAPS WERE ALSO REPLACED.  I BELIEVE I HAD SHOTS BEFORE RECAPPING, BUT I THINK THEY MAY BE LOST.

admcolafter
admcolafter
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admcolbeforesurgery
admcolbeforesurgery
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   SHOT OF THE SET AFTER FIRST POWERUP BEFORE RECAPPING. 

   SHOT AFTER REMOVING THE CATARACT FROM THE CRT.

   I DID A SECOND SOFT START AFTER RECAPPING, THIS TIME ON THE TEST RIG.  THE PICTURE HAD SEVERE GHOSTING.  BOTH TUBES ON THE TUNER HAD SEVERE HEATER/CATHODE LEAKAGE AND WERE REPLACED.  THE GHOSTING WAS LATER DETERMINED TO BE A BAD DELAY LINE.

  I DID GET AN OVERALL DECENT PIC ON THE RIG, BUT NOT ON THE SET'S OWN TUBE.  I LATER CONFIRMED THE TUBE WAS GETTING GASSY.  I BEGAN LOOKING FOR A REPLACEMENT.  THE NEXT PICS SHOW HOW BAD THE CRT WAS GETTING.

admcolcrtafter
admcolcrtafter
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admcolorwork2
admcolorwork2
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archierasp1
archierasp1
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